Journal:
Problem Statement:
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Design, build, test, and race a transportation vehicle
(called a Mousetrap Racecar).
Design Requirements:
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Use a standard mousetrap.
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Car cannot have manufactured wheels.
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Car must be made at home.
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Car must use found or scrounged materials.
My Design Objectives:
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Car must be built sturdy enough to make multiple runs
over the starting line.
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Car may be built for speed (velocity) or distance (velocity*
time).
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F(Force)=M(mass)*A(acceleration) therefore the mousetrap
provides a standard unit of force (F=1) and if my design is heavier, the
acceleration will decrease which equals lower speed. If my design is lighter,
the acceleration will increase which equals a higher speed. To make my
car go farther, I need to keep force (F=1) acting throughout a longer period
of time because V(velocity)*T(time)=D(distance).
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My design objective will be to try to maximize the
period of time that the spring force of the mousetrap acts upon the wheels.
My Hypothesis:
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I predict that the lighter my car is the farther it
will go.
Steps to Create Car:
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I have started searching for my materials by looking
at old toys. I located an old Erector set that still has many mechanical
brackets and parts. I found some old computer CD-ROMs. I went to Giant
and bought a mousetrap. I also bought Epoxy and some string. I raided my
mother’s sewing box and found some spools and I pulled all of the thread
off of them. I asked my dad for help when using Epoxy and drilling holes.
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I drew my first designs (Figure 1 — First Design and
Concept). I drew my first design using 3 wheels because it is lighter and
sturdier than 4 wheel designs.
Figure
1 — First Design and Concept
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I decided to use old CD-ROMs for my wheels. My first
problem was that the middle holes ire too large (Figure 2 — Wheels made
from CD-ROMs). Because of that, I looked through an old Erector set and
found 2 gears. I centered the gears and I glued them in place with 5 minute
Epoxy (which takes 3 hours to get hard).
Figure 2 — Wheels
made from CD-ROMs
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While waiting for the wheels to dry, I decided to find
out how far the mousetrap spring traveled (Figure 3 — Distance Traveled
By Mousetrap Lever). I will use this information to size my pulley string.
Figure 3 — Distance
Traveled By Mousetrap Lever
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I performed an experiment to see how far the string
would be pulled when the mousetrap was set off and moved through a half-circle
(Figure 4 — Distance Traveled by String Attached to Lever).
Figure 4 — Distance
Traveled by String Attached to Lever
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I then built a frame for my car (Figure 5 — Frame Layout).
It’s called a ladder frame because it looks like a ladder. I first used
screws to bolt it together to see if everything fit. After final fitting
(Figure 6 — Final Layout of Mousetrap Car), I removed the screws and used
pop rivets to securely fasten everything together. I received help with
the pop rivet gun from my dad.
Figure 5 — Frame
Layout
Figure 6 — Final
Layout of Mousetrap Car
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To make the rear axle and pulley, I cut 2 rubber grommets
so that they would fit inside a small spool (Figure 7 — Rear Axle, Pulley,
and Grommets). I pushed the axle into the grommets exactly halfway. I measured
it to 28 millimeters on each side of the axle so it would be exactly in
the center. Then I used Epoxy to attach the pieces together so they would
not move around (Figure 8 — Pulley and Axle Assembly after Epoxy Glue).
Figure 7 — Rear Axle,
Pulley, and Grommets
Figure 8 — Pulley
and Axle Assembly after Epoxy Glue
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I assembled our front wheel (Figure 9 — Front Wheel
Assembly). The axle diameter was too small for the spool’s internal diameter.
I epoxied 2 #10 washers to the spool so the axle would not slip around
as much.
Figure 9 — Front
Wheel Assembly
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I measured the mousetrap to make sure it was going
to be in the centerline of the car. I drilled 2 holes in the mousetrap.
Again I used pop rivets to attach the trap to the vehicle. Then I cut a
length of string, and attached it to the lever arm on the mousetrap. (Figure
10 — Mousetrap Positioning).
Figure 10 — Mousetrap
Positioning
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I attached the front wheel (Figure 9 — Front Wheel
Assembly) and the rear pulley assembly (Figure 7 — Rear Axle, Pulley, and
Grommets) to the frame of the car. I completed the final pop riveting and
then I epoxied the front wheel assembly to prevent the axle from sliding.
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I applied Epoxy to all of the pop rivet joints (Figure
11 — Detail of Front of Car Showing Epoxy) because of a problem, that the
rear cross frame was moving.
Figure
11 — Detail of Front of Car Showing Epoxy
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I attached the rear wheels to the car (Figure 12 —
Top View of Vehicle) and my dad cut a notch in the pulley to secure the
string. The vehicle was now complete and ready for its first test run.
Figure 12 — Top View
of Vehicle
February 27, 2000
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I began my runs. I used a hallway in my house on a
regular wood floor (Figure 13 - Starting Line). I set up a starting line
so the cars would all start in the same place. I used a Synchrotimer®
X-1000 stopwatch, which was capable of measuring to 1/100 of a second.
My dad operated the stopwatch so I could set off my car and measure distances.
Figure 13 - Starting
Line
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We began our runs (Figure
14 — Test Runs). I made ten runs because I could figure out the average
and minimizing errors in timing, measuring distances, and errors in the
mousetrap’s spring. I figured out my average speed by D(distance)/T(time).
The car’s average speed was 92.1 cm/s.
Figure 14 — Test
Runs
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I found some problems in the Test Run (Figure 14 —
Test Runs). The first problem I saw was the string wrapped around the axle
sometimes. Another problem was the string came off the wheels and didn’t
come off the spool. The other problem I saw was the wheels didn’t have
enough friction. To solve these problems, I have to figure out a way to
keep the string in the center of the mousetrap lever. To fix the friction
problem, I will try adding a softer material, which has more friction,
like a rubber band.
Figure 15 — Rubber Bands
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I ran the car after fixing the mistakes (Figure 16
— Second Trial Run). The string kept catching on the spool, so my dad cut
a larger hole in it. It worked much better. The average speed improved.
Figure 16 — Second
Trial Run
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I put an entire can of play-do on the back of the car
(Figure 17 — Play-Do) to see if my hypothesis was correct. It was correct
because it went much slower, but it also went much farther(Figure 18 —
Test Runs with Heavier Weight).
Figure
17 — Play-Do

Figure 18 — Test Runs
with Heavier Weight
March 19, 2000
Problem:
1. Dropped Mousetrap Racecar and broke rear wheel
in half (Figure 19 — Broken Wheel).
Materials (Figure 20 — Repaired Broken Wheel):
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Quickset Epoxy
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CD-ROM
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Axle Hub
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Screw
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Allen Wrench
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Diagonal Cutters
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Plastic
Procedure:
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I removed broken wheel and screw with Allen Wrench.
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I used Diagonal Cutters to cut through and remove old
Epoxy in axle hub although I got some help because I was not strong enough.
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I mixed up Epoxy according to directions.
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I then placed axle hub on plastic so it will not stick
to other surfaces.
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Then I attached axle hub to CD-ROM using Epoxy.
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I waited 3 hours for Epoxy to dry.
Conclusion:
-
Although the wheels worked, I’m going for a longer
distance by adding larger wheels.
Figure 19 — Broken
Wheel
Figure
20 — Repaired Broken Wheel
Problem:
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Racecar didn’t go as far as it could because the back
drive wheels are too small.
Materials:
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Quickset Epoxy
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Plastic Plates
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Back wheels
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Drill
Procedure:
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I measured the plates to find the center.
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I drilled a hole in the plate.
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I then applied Epoxy to the plastic plate and attached
the wheels.
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I waited 3 hours for the Epoxy to dry.
Conclusion:
1. The wheels were larger (Figure 21 — Wheels) and
could go farther than the small wheels with the same amount of force. They
still spin and I can’t find any rubber bands, which will fit over the wheels.
Figure 21 — Wheels
Problem:
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Racecar didn’t have as much traction because of the
plastic plates.
Materials:
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Wrench
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Play-Doh (Figure 22 — Play-Doh)
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Car
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Screws
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Erector-Set pieces
Procedure:
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I attached an Erector piece to the back of my car with
a wrench, bolts, and screws.
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I then placed purple play-doh to the back of the car.
Conclusion:
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The car works better but it is still spinning too much.
Figure 22 — Play-Doh
Problem:
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The racecar’s wheels are spinning out of control although
they are better because of the play-doh.
Materials:
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Car
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Electrical Tape
Procedure:
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I attached the electrical tape (Figure 23 — Electrical
Tape) to the wheels of the car.
Conclusion:
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The car is much better but it is popping wheelies,
which are losing energy.
Figure 23 — Electrical
Tape
Problem:
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The car is popping wheelies and losing energy because
of them.
Materials:
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Play-Doh
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Car
Procedure:
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I removed about 1/2 of the play-doh (Figure 24 — Less
Play-Doh).
Conclusion:
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The car goes farther and faster because of more energy
added to the car instead of the wheels.
Figure 24 — Less
Play-Doh
Problem:
1. Wheels are sliding back and forth across the
axle because they are too loose so they must be tightened.
Materials:
1. Allen Wrench
2. Car
Procedure
1. I tightened the screws on car wheels and then
got my dad to tighten them even more.
2. Rerun car ().
Conclusion:
1. It helped the wheels go straight but they are
very slow.
Figure 25 - Trial Run 1
Problem:
1. The racecar goes very slow which is probably
because now there is too much weight on the car.
Materials:
1. Car
2. Play-Doh
Procedure:
1. I removed play-doh from back of car so it would
go faster.
2. Rerun Car (Figure 26 - Trial Run 2)
Conclusion:
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The smaller weight helped the car move faster so my
car is done (Figure 27 - Final Car).
Figure 26 - Trial
Run 2
Figure 27 - Final
Car